Fuel System
Changes
February, 2006 - All of this
modification really started with my desire for cooler engine temperatures. "So
what does the fuel system have to do with that?" you may ask. Other than my fuel
injection unit being in the way of my air intake, nothing. But I had a plan to
remount the fuel injection and one thing led to another and well...
First off, my fuel injection unit has
performed pretty well in its current configuration. But it lays right in the
middle of my air intake scoop/NACA duct and I figure that its blocking a lot of
cooling air. I did a little "eye-balling" of the unit and determined that if I
could turn it upside down It would clean up the lower part of the cowl nicely
and let the air in without as much interference. In order to rotate the unit 180
degrees I would need to drop the intake elbow about 1-1/2 inches so that the
fuel metering mechanism could clear the engine oil sump. Airflow Performance
built be a nice phenolic adapter to drop the elbow, so I installed the adapter
and turned the fuel injection unit 180 degrees.


With the unit down rotated from its previous
location, I had to re-route the throttle and mixture cables. Unfortunately, the
new locations put them right where the electric fuel pump was located on the
firewall. Well, I never had liked the pump on the firewall, so I decided to move
it. I chose the inside of the firewall in the lower gear well area for its new
location, but that was where the fuel filter was located. OK, I never liked that
there either because it was difficult to check the filter. Now is the time
to move it too, so I decided to locate it in the rear armrest.
With all the decisions made on where the new
locations for everything where, I unbolted the pump and filter and started
remounting them. The filter needed to have the fuel line running from the fuel
selector to the firewall cut and fitting attached, so that was the first job.
After installation it looks like this.

Next I attached the pump to the inside
firewall and plumbed new tubing to the firewall bulkhead fitting. This was a
tight fit, but I shouldn't have to do much with it once its installed, so the
remote location is OK.


I could now run the throttle and mixture
cables through the firewall in their new locations. I re-oriented the throttle
and mixture arms to get the correct actuation and then made a bracket to secure
the cables as they came through the firewall.
The fuel line attachments from the firewall
bulkhead to the engine fuel pump where pretty straightforward. Without the pump
in the way the firewall looks much simpler. From the engine driven fuel pump to
the fuel controller I connected a short hose. I installed a bracket to support
the fuel flow meter to the air intake elbow and then ran a hose from the
controller to the fuel flow meter. From the fuel flow meter to the new flow
divider I attached another hose. Here is the fuel flow meter and bracket mounted
to the elbow.

My Lycoming engine runs great at high RPM's
but can stumble and spurt at low RPM's. In investigating this I came upon an
interesting discovery on James Redmon's
Berkut site. He had similar issues at low RPM and found that by replacing
the fuel distribution block with a flow divider solved his problem and he can
now run at smooth idle as low as 700-750 RPM. I called the good folks at Airflow
Performance and discussed this with them and while they say the distribution
block should normally be fine, the flow divider is more precise at separating
the flow of fuel to the individual nozzle lines and could be retrofit fairly
easily. I ordered the flow divider and then went about figuring where to mount
it. Here is a picture of the old distribution block (right) still attached to
it's mounting plate and the new flow
divider (left).

The rear of the oil sump looked like the best location to
mount a bracket and still be able to connect the fuel lines than I had with the
previous arrangement. I test fit a paper template of the bracket and then
attached the permanent one.

After removing the fuel lines and rearranging them to get the
right lengths for the new location, I attached each end to the flow divider.
Finally, the fuel system modification is complete! Here's a pictures of the
final result.

And another one showing the installation with the oil cooler
mounted - a little crowded, but it works!

Last Updated on
July 12, 2008
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